Tuesday, July 17, 2012

LDRS 31: My Flights

LDRS 31 was at the local flying field for me this year in Potter, NY and spanned July 12th through 16th. I was there on all 5 days, flying rockets on the first 4. Though I only launched 5 times, it was the most total impulse for me at one launch. The weather was absolutely perfect: clear skies and light winds (though it was uncomfortably hot every day but it's supposed to be that way for a rocket launch).

LDRS is such a busy event (with 269 fliers registered, and many of which were way cooler flights than mine), that I did not focus on collecting pictures or videos of my launches. That being said, all I really have is some data from 3 flights with my new Perfectlfite altimeters and 1 onboard video from Positive Ascent.

So here's the recap of my launches day by day:
_________________________________________________________________________________
Thursday July 12th, 2012:

I launched my 29mm Minimum Diameter rocket on the I224 Classic motor. It was about as disappointing as one (especially me) would expect....

Here's what happened:

It took off extremely hard as expected but immediately corkscrewed violently (just like what ended the Super Weasel a couple months ago). At about 1000 feet it finally broke into two - the booster with motor casing arcing over gracefully to the east according to some witnesses, and the top half with the tracker and altimeter falling surprisingly near the pad where it took off. It took a while to track the signal to finally find the top half of the rocket. The booster is still lost but it wasn't a big deal as that motor hardware was only around $50 and I replaced it right away.

Here's where it got more interesting. When I went to retrieve my launch pad (the custom tower I built for this rocket) I was incredibly surprised to find that it was in 4 pieces on the ground.

Here are a few post-shred pictures of what's left:





Given the flight path and condition of the pad, I determined that the pad either failed instantly, causing the corkscrew, or the rocket caught on the pad, ripping it to pieces and causing the corkscrew. The corkscrewing followed by a shred produced nothing but erroneous data on the altimeter so no velocity or altitude data was taken from the flight.

_________________________________________________________________________________
Friday July 13th, 2012:

After a not-unexpected, but still disappointing failure on Thursday, I launched a couple more conventional rockets on Friday.

First up was my X-Calibur, which was my first high power rocket and is somewhere in the vicinity of 12 years and 30 flights old. Since I now have a reliable tracking system, I put in way more motor than I previously would have. I selected an I243 White motor from CTI. It was a perfect straight and fast boost to about 560 miles per hour. The altimeter recorded 4300 feet. Even with single deployment, the rocket came almost straight down a couple hundred yards away for an easy recovery. 

Here's the plot that I made from the data from the Pnut altimeter:



After the success from the X-Calibur, I decided to go a little bigger. I loaded up a CTI K360 White motor into my Eclipse. At 1281 Newton-seconds, this is the most total impulse that will fit into that rocket. The motor provided a beautiful straight boost and the Eclipse had a picture perfect launch to 5401 feet. 

When Clare and I were walking back from recovering the Eclipse, people from the Science/Discovery channel (they were there the whole launch too, more on that later) were filming us and had us sign release forms just in case they decide to use that shot on the TV special of LDRS.
_________________________________________________________________________________
Saturday July 14th, 2012:
This is the busiest day of LDRS, and I decided to launch Positive Ascent on the bigger of the 2 motors I had prepped for its 10th flight. With clear skies and low winds there was no reason not to. I flew without the camera bay on a 5 grain M1670 Blue Streak. It was an absolutely perfect straight up launch. We followed it until the drogue charges separated it at apogee. It wasn't until the main popped at 900 feet a couple minutes later that we saw it right again. It was coming in hard right behind the row of trees behind the flight line. The pilot chute was open but the deployment bag for the main parachute was tangled enough where the chute wasn't releasing. After what seemed like an eternity, the main opened suddenly with only about 400 feet left with the pilot chute slightly tangled up in the main's lines still. The rocket landed softly in a field just on the other side of the treeline near the parking area. The rocket had reached an altitude of 9900 feet, a few hundred feet higher than expected and just under mach 1.



_________________________________________________________________________________
Sunday July 15th, 2012:
Sunday started with a few light rain showers but I sat and prepped Positive Ascent for a lower 11th flight anyway. Sure enough the rain passed, the clouds passed, and for the 4th day we had perfect rocket weather. This time, Positive Ascent was ready to go with the camera bay installed. It flew on a 54mm L805 White motor. It was another perfectly straight up flight and recovered perfectly in the field this time. It reached 3300 feet so the video isn't that spectacular, but it is still cool.












No comments:

Post a Comment